16 Commits (25d46974e3a92c9d88bdb053b557a7d074ac5909)

Author SHA1 Message Date
Penguin 25d46974e3 partially fixed issue where motor controller was seeing a chirp on the RX line, causing some start bytes to be seen as a combination of the start byte and the src addr byte. Only partially fixed because the buffer stream is still skipped occasionally. Its just not due to that issue. The issue was fixed by driving the max485 chips with 5v at vcc instead of 3.3 3 years ago
Penguin 9f0877c746 fixed issue with receiving data. the interrupt overhead was too high so i switch to an interrupt/polling hybrid. idk how im going to do the queue but i have the library finished 3 years ago
Penguin 4bc852b44a weird behavior... message handling not working currently 3 years ago
Penguin b5ef056990 testing protocol 3 years ago
Penguin 310e5a1a32 using circular buffer from penguin buffer until i implement ring buffer 3 years ago
Penguin 252037532b rs485 working. had to switch to different pins because something was running some frequency on d13. annoyed. 3 years ago
Penguin 4751793db5 rs485 not working as expected 3 years ago
Penguin 6988019971 fixing line endings, removing PA08 PA09 from pins 3 years ago
Penguin a6db0bddef added rs485 usart1 3 years ago
Penguin ce63792708 trying some wacky ways to determine speeds and direction. eventually ill look up some algorithms to do this properly. for now im goofin 3 years ago
Penguin 807f7c29e8 added 250hz timer for giving motor updates 3 years ago
Penguin feb61e56a8 accidentally removed p_uart_init() via code generation... added it back 3 years ago
Penguin 51e6edb355 figured out which pins were which on the motor controller board... im using a random one from a hobby shop i bought forever ago and have no documentation 3 years ago
Penguin 49fbfa2cc4 added a printf 3 years ago
Penguin bdabdde746 fuck windows line endings honestly 3 years ago
Penguin 6758c57836 pwm working 3 years ago